Show and Shine Discuss the latest aero kits, and other non-performance items in here.

picked up an s14,its definitely a little different, needs some stuff, check it out

Old Dec 27, 2009 | 02:03 PM
  #196  
alex_s817's Avatar
Thread Starter
Registered User
 
Joined: Oct 2007
Posts: 111
From: Cincinnati Ohio
it runs!

wont idle though, running super rich. also im out in utah right now with the car and the altitude + cold weather cant be helping... if anyone has any input as to how to set the injector sizing with the emanage ultimate, please help me out.

Last edited by alex_s817; Jan 20, 2010 at 06:43 PM.
Old Dec 28, 2009 | 06:31 AM
  #197  
1SXY240's Avatar
Registered User
 
Joined: Oct 2009
Posts: 173
From: Dallas, TX
Nice! Get the car idling good, and loom the wires! I wanna see more videos haha
Old Jan 6, 2010 | 09:37 AM
  #198  
nissandrift's Avatar
Registered User
 
Joined: Feb 2004
Posts: 114
From: Raleigh, NC
Sounds pretty good... so when will the car be coming back this direction?
Old Jan 7, 2010 | 03:01 AM
  #199  
japanesenut's Avatar
Registered User
 
Joined: Dec 2008
Posts: 182
From: missouri
nice setup .
Old Jan 12, 2010 | 09:19 AM
  #200  
alex_s817's Avatar
Thread Starter
Registered User
 
Joined: Oct 2007
Posts: 111
From: Cincinnati Ohio
thanks.

well ive gotten a lot done in the past few weeks, both good and bad things have come about.

i had to pull the dash from the car again because the running lights suddenly stopped working. i fixed that problem and got everything back in. i changed the diff fluid with mobil 1, the tranny with redline mt 90, and bled the brakes. i had to buy new sending units for the gauges because the current ones were not reading. i added a 6k hid kit, yellow high beam bulbs, new lug nuts, a broadway 270mm rear view mirror, new general exclaim uhp tires, a 3 inch flex section on the exhaust, an aem uego wideband, and some other little things. i also added a 150 amp breaker in place of the 80 amp inline fuse i had on the battery power wire.

after a lot of little problems here and there, i got it running as you can see in the video above. i drove the car 2 and a half hours to las vegas to get it tuned. Doug at Doug's Dyno Power in Henderson, Nevada does a great job and I recommend him to anyone. The car was super rich with the AFRs in the low 9's on the first pull. car made 75whp on the first run! haha. after a little bit, cylinder six stopped firing and I had to get the car off of the dyno because other people were waiting. I must have loomed the engine harness too tight, causing a wire to break. i ran a new, temporary wire from the ecu to the ignitor which fixed the problem. The car had made 186 whp on 15 psi on 5 cylinders, and once fixed, it made 249whp at 11 psi on a mustang dyno with the afrs still pretty rich in the low 11's - high 10's and revving to only 5k. The car had been sputtering before due to the 6th cylinder not firing. This sputtering masked the boost cut that was happening due to the stock map sensor. 11 psi ended up being where we stopped until i can get a gm 3 bar. perfect for a low boost setting but no where near what i want. i got everything loaded up and headed out to north carolina. about 5 hours in, two of the driver's side rear wheel studs snapped off at about 80 mph. i pulled over in time and the wheel was about to fall off. after the tow truck fees and the crazy labor prices, i realized if it breaks down again i wouldnt have enough money on me to fix it. i drove the car back and parked it til summer. definitely sucks but this will give me time to save money for more parts and ill be able to fix every little problem this summer.

pics and dyno vid will be posted shortly

Last edited by alex_s817; Jan 16, 2010 at 11:05 PM.
Old Jan 12, 2010 | 11:46 PM
  #201  
alex_s817's Avatar
Thread Starter
Registered User
 
Joined: Oct 2007
Posts: 111
From: Cincinnati Ohio
flex pipe




circuit breaker


rolled rear fenders


loomed engine harness


wide band


new tires




harness in, looks alright, kinda gay but whatever at this point


yellow high beams


on the dyno


he said he had never had a car on the dyno with a bike on it ....


the car that went after me. e85, gt3071, full defi cluster, very nice drift car




i like these mirrors a lot


Old Jan 13, 2010 | 07:15 AM
  #202  
Nickmerrone's Avatar
Registered User
 
Joined: Jan 2009
Posts: 880
From: Langhorne, PA
short shifter..naow! haha
Old Jan 13, 2010 | 09:45 AM
  #203  
1SXY240's Avatar
Registered User
 
Joined: Oct 2009
Posts: 173
From: Dallas, TX
dang that shifter is huge! lol
Old Jan 13, 2010 | 12:45 PM
  #204  
alex_s817's Avatar
Thread Starter
Registered User
 
Joined: Oct 2007
Posts: 111
From: Cincinnati Ohio
yeah ill change it once i get everything else working right. there is a pretty noticeable vibration coming from somewhere in the drivetrain. the clutch needs to be replaced for sure and possibly the tranny too.
Old Jan 16, 2010 | 11:06 PM
  #205  
alex_s817's Avatar
Thread Starter
Registered User
 
Joined: Oct 2007
Posts: 111
From: Cincinnati Ohio


Old Jan 20, 2010 | 08:04 AM
  #206  
lalo's Avatar
Registered User
 
Joined: Nov 2007
Posts: 5
From: NORTH CAROLINA
your doing a good job keep it up do your thing man
Old Jan 20, 2010 | 06:41 PM
  #207  
alex_s817's Avatar
Thread Starter
Registered User
 
Joined: Oct 2007
Posts: 111
From: Cincinnati Ohio
thanks man, its gettin there
Related Topics
Thread
Thread Starter
Forum
Replies
Last Post
Sqwibbs
Wheels and Tires
16
Jul 1, 2007 10:02 AM
leiferik1
Off-Topic
5
Jun 5, 2003 02:47 PM
TekonMotors
Private For Sale / Wanted
10
Mar 10, 2003 08:48 PM
leiferik1
Off-Topic
20
Jul 28, 2002 01:26 AM


Thread Tools
Search this Thread

All times are GMT -7. The time now is 02:05 PM.